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Friday, April 5, 2024

Fukushima nuclear accident

From Wikipedia, the free encyclopedia
 
Fukushima nuclear accident
Part of the 2011 Tōhoku earthquake and tsunami
The four damaged reactor buildings (from left: Units 4, 3, 2, and 1) on 16 March 2011. Hydrogen-air explosions in Units 1, 3, and 4 caused structural damage.
Date11 March 2011; 13 years ago
LocationŌkuma and Futaba, Fukushima, Japan
Coordinates37°25′17″N 141°1′57″E
OutcomeINES Level 7 (major accident)
Deaths1 suspected from radiation (lung cancer, 4 years later), and up to 2,202 from evacuation-related stress among the elderly.
Non-fatal injuries6 with cancer or leukemia,
16 with physical injuries due to hydrogen explosions.
2 workers hospitalized with radiation burns
Displaced+164,000 local residents
Cross-section of a typical BWR Mark I containment as used in units 1 to 5.
RPV: reactor pressure vessel
DW: drywell enclosing reactor pressure vessel
WW: wetwell – torus-shaped all around the base enclosing steam suppression pool. Excess steam from the drywell enters the wetwell water pool via downcomer pipes.
SFP: spent fuel pool area
SCSW: secondary concrete shield wall

The Fukushima nuclear accident was a major nuclear accident at the Fukushima Daiichi nuclear power plant in Ōkuma, Fukushima, Japan which began on March 11, 2011. The proximate cause of the accident was the 2011 Tōhoku earthquake and tsunami, which resulted in electrical grid failure and damaged nearly all of the power plant's backup energy sources. The subsequent inability to sufficiently cool reactors after shutdown compromised containment and resulted in the release of radioactive contaminants into the surrounding environment. The accident was rated seven (the maximum severity) on the INES by NISA, following a report by the JNES (Japan Nuclear Energy Safety Organization).

No adverse health effects among Fukushima residents or power station workers have been documented that are directly attributable to radiation exposure from the accident, according to the United Nations Scientific Committee on the Effects of Atomic Radiation. Insurance compensation was paid for one death from lung cancer, but this does not prove a causal relationship between radiation and the cancer. 6 other persons have been reported as having developed cancer or leukemia. 2 workers were hospitalized because of radiation burns, and several other people sustained physical injuries as a consequence of the accident. Criticisms have been made about the public perception of radiological hazards resulting from accidents and the implementation of evacuations (similar to the Chernobyl nuclear accident), as they were accused of causing more harm than they prevented. Following the accident, at least 164,000 residents of the surrounding area were permanently or temporarily displaced (either voluntarily or by evacuation order). This response resulted in at least 51 fatalities, with more in following estimates, mainly attributed to subsequent stress or fear of radiological hazards, among older people for the most part.

Investigations faulted lapses in safety and oversight, namely failures in risk assessment and evacuation planning. Controversy surrounds the disposal of treated wastewater once used to cool the reactor, resulting in numerous protests in neighboring countries.

Background

Aerial view of the station in 1975, showing separation between units 5 and 6, and 1–4. Unit 6, completed in 1979, is seen under construction.

The Fukushima Daiichi Nuclear Power Plant consisted of six General Electric (GE) light water boiling water reactors (BWRs). Unit 1 was a GE type 3 BWR. Units 2-5 were type 4. Unit 6 was a type 5. During the 12-year construction of the power station, improvements in technology and design allowed for improvements to be made in the reactors which were constructed sequentially (beginning with unit 1, ending with unit 6).

At the time of the Tōhoku earthquake on 11 March 2011, units 1–3 were operating. However, the spent fuel pools of all units still required cooling.

Materials

Many of the internal components and fuel assembly cladding are made from a zirconium alloy (Zircaloy) for its low neutron cross-section. At normal operating temperatures (~300 °C (572 °F), it is inert. However, above 1,200 degrees Celsius (2,190 °F), Zircaloy can be oxidized by steam to form hydrogen gas or by uranium dioxide to form uranium metal. Both of these reactions are exothermic. In combination with the exothermic reaction of boron carbide with stainless steel, these reactions can contribute to the overheating of a reactor.

Isolated cooling systems

In the event of an emergency situation, reactor pressure vessels (RPV) are automatically isolated from the turbines and main condenser and are instead switched to a secondary condenser system which is designed to cool the reactor without the need for pumps powered by external power or generators. The isolation condenser (IC) system involved a closed coolant loop from the pressure vessel with a heat exchanger in a dedicated condenser tank. Steam would be forced into the heat exchanger by the reactor pressure, and the condensed coolant would be fed back into the vessel by gravity. Each reactor was initially designed to be equipped with two redundant ICs which were each capable of cooling the reactor for at least 8 hours (at which point, the condenser tank would have to be refilled). However, it was possible for the IC system to cool the reactor too rapidly shortly after shutdown which could result in undesirable thermal stress on the containment structures. To avoid this, protocol called for reactor operators to manually open and close the condenser loop using electrically operated control valves.

After the construction of unit 1, the following units were designed with new open-cycle reactor core isolation cooling (RCIC) systems. This new system utilized the steam from the reactor vessel to drive a turbine which would power a pump to inject water into the pressure vessel from an external storage tank to maintain the water level in the reactor vessel and was designed to operate for at least 4 hours (until the depletion of coolant or mechanical failure). Additionally, this system could be converted into a closed-loop system which draws coolant from the suppression chamber (SC) instead of the storage tank, should the storage tank be depleted. Although this system could function autonomously without an external energy source (besides the steam from the reactor), DC power was needed to remotely control it and receive parameters and indications and AC power was required to power the isolation valves.

In an emergency situation where backup on-site power was partially damaged or insufficient to last until a grid connection to off-site power could be restored, these cooling systems could no longer be relied upon to reliably cool the reactor. In such a case, the expected procedure was to vent both the reactor vessel and primary containment using electrically or pneumatically operated valves using the remaining electricity on site. This would lower the reactor pressure sufficiently to allow for low-pressure injection of water into the reactor using the fire protection system in order to replenish water lost to evaporation.

On-site backup power

In the event of a loss of off-site power, emergency diesel generators (EDG) would automatically start in order to provide AC power. Two EDGs were available for each of units 1–5 and three for unit 6. Of the 13 EDGs, 10 were water-cooled and placed in the basements about 7–8 m below the ground level. The coolant water for the EDGs was carried by a number of seawater pumps placed on the shoreline which also provide water for the main condenser. These components were unhoused and only protected by the seawall. The other three EDGs were air-cooled and were connected to units 2, 4, and 6. The air-cooled EDGs for units 2 and 4 were placed on the ground floor of the spent fuel building, but the switches and various other components were located below, in the basement. The third air-cooled EDG was in a separate building placed inland and at higher elevation. Although these EDGs are intended to be used with their respective reactors, switchable interconnections between unit pairs (1 and 2, 3 and 4, and 5 and 6) allowed reactors to share EDGs should the need arise.

The power station was also equipped with backup DC batteries kept charged by AC power at all times, designed to be able to power the station for approximately 8 hours without EDGs. In units 1, 2, and 4, the batteries were located in the basements alongside the EDGs. In units 3, 5, and 6, the batteries were located in the turbine building where they were raised above ground level.

In the late 1990s, three additional EDGs were placed in new buildings located inland and at higher elevation to comply with new regulatory requirements, but the switching stations that connected the EDGs to units 1–5 were located in the turbine buildings. Only the switching station for unit 6 was inside of the reactor building.

Fuel inventory

The units and central storage facility contained the following numbers of fuel assemblies:

Location Unit 1 Unit 2 Unit 3 Unit 4 Unit 5 Unit 6 Central storage
Reactor fuel assemblies 400 548 548 0 548 764 N/A
Spent fuel assemblies 292 587 514 1331 946 876 6375
Fuel type UO
2
UO
2
UO
2
/MOX
UO
2
UO
2
UO
2
UO
2
New fuel assemblies 100 28 52 204 48 64 N/A

In September 2010, Reactor 3 was partially fueled by mixed-oxides (MOX). There was no MOX (mixed oxide) fuel in any of the cooling ponds at the time of the incident.

Earthquake tolerance

The original design basis was a zero-point ground acceleration of 250 Gal and a static acceleration of 470 Gal, based on the 1952 Kern County earthquake (0.18 g, 1.4 m/s2, 4.6 ft/s2). After the 1978 Miyagi earthquake, when the ground acceleration reached 0.125 g (1.22 m/s2, 4.0 ft/s2) for 30 seconds, no damage to the critical parts of the reactor was found. In 2006, the design of the reactors were reevaluated with new standards (which included vertical acceleration and differentiated E/W and N/S motion) which found the reactors would withstand accelerations ranging from 412 Gal to 489 Gal.

Accident

The height of the tsunami that struck the station approximately 50 minutes after the earthquake.
A: Power station buildings
B: Peak height of tsunami
C: Ground level of site
D: Average sea level
E: Seawall to block waves

Earthquake

The 9.0 MW earthquake occurred at 14:46 on Friday, 11 March 2011, with the epicenter off of the east coast of the Tōhoku region. It produced maximum ground g-forces of 0.56, 0.52, 0.56 at units 2, 3, and 5 respectively. This exceeded the seismic reactor design tolerances of 0.45, 0.45, and 0.46 g for continued operation, but the seismic values were within the design tolerances at units 1, 4, and 6.

Upon detecting the earthquake, all three operating reactors (units 1, 2, and 3) automatically shut down. Due to expected grid failure and damage to the switch station as a result of the earthquake, the power station automatically started up the EDGs, isolated the reactor from the primary coolant loops, and activated the emergency shutdown cooling systems.

Tsunami and loss of power

The largest tsunami wave was 13–14 m (43–46 feet) high and hit approximately 50 minutes after the initial earthquake, overtopping the seawall and exceeding the plant's ground level, which was 10 m (33 ft) above the sea level.

The waves first damaged the seawater pumps along the shoreline, disabling the 10 water cooled EDGs. The waves then flooded all turbine and reactor buildings, damaging EDGs and other electrical components and connections located on the ground or basement levels at approximately 15:41. The switching stations that provided power from the three EDGs located higher on the hillside also failed when the building that housed them flooded. One air cooled EDG, that of unit 6, was unaffected by the flooding and continued to operate. The DC batteries for units 1, 2, and 4 were also inoperable shortly after flooding.

As a result, units 1–5 lost AC power and DC power was lost in units 1, 2, and 4. In response, the operators assumed a loss of coolant in units 1 and 2, developing a plan in which they would vent the primary containment and inject water into the reactor vessels with firefighting equipment. TEPCO notified authorities of a "first-level emergency".

Two workers were killed by the impact of the tsunami.

The dry cask storage building was also flooded, causing some concerns about possible damage.

Reactors

Unit 1

The isolation condenser (IC) was functioning prior to the tsunami, but the DC-operated control valve outside of the primary containment had been in the closed position at the time to prevent thermal stresses on the reactor components. This status was uncertain at the time due to a loss of indications in the control room, who had correctly assumed loss of coolant (LOC). 3 hours later, the plant operators attempted to manually open the control valve, but the IC failed to function, suggesting that the isolation valves were closed. Although they were kept open during IC operation, the loss of DC power in unit 1 (which occurred shortly prior to the loss of AC power) automatically closed the AC-powered isolation valves in order to prevent uncontrolled cooling or a potential LOC. Although this status was unknown to the plant operators, they correctly interpreted the loss of function in the IC system and manually closed the control valves. The plant operators would continue to periodically attempt to restart the IC in the following hours and days, but it did not function.

The plant operators then attempted to utilize the building's fire protection (FP) equipment, operated by a diesel-driven fire pump (DDFP), in order to inject water into the reactor vessel. A team was dispatched to the reactor building (RB) in order to carry out this task, but the team found that the reactor pressure had already increased significantly to 7 MPa, which was many times greater than the limit of the DDFP which could only operate below 0.8 MPa. Additionally, the team detected high levels of radiation within the RB, indicating damage to the reactor core, and found that the primary containment vessel (PCV) pressure (0.6 MPa) exceeded design specifications (0.528 MPa). In response to this new information, the reactor operators began planning to lower the PCV pressure by venting. The PCV reached its maximum pressure of 0.84 MPa at 02:30, after which it stabilized around 0.8 MPa. Venting of the PCV was completed later that afternoon at 14:00.

At the same time, pressure in the reactor vessel had been decreasing to equalize with the PCV, and the workers prepared to inject water into the reactor vessel using the DDFP once the pressure had decreased below the 0.8 MPa limit. Unfortunately, the DDFP was found to be inoperable and a fire truck had to be hooked up to the FP system. This process took about 4 hours, as the FP injection port was hidden under debris. The next morning (March 12, 04:00), approximately 12 hours after loss of power, freshwater injection into the reactor vessel began, later replaced by a water line at 09:15 leading directly from the water storage tank to the injection port to allow for continuous operation (the fire engine had to be periodically refilled). This continued into the afternoon until the freshwater tank was nearly depleted. In response, injection stopped at 14:53 and the injection of seawater, which had collected in a nearby valve pit (the only other source of water), began.

Power was restored to unit 1 (and 2) using a mobile generator at 15:30 on March 12.

At 15:36, a hydrogen explosion damaged the secondary confinement structure (the RB). The cause was unknown to the workers at the time, most of whom evacuated shortly after the explosion. The debris produced by the explosion damaged the mobile emergency power generator and the seawater injection lines. The seawater injection lines were repaired and put back into operation at 19:04 until the valve pit was nearly depleted of seawater at 01:10 on the 14th. The seawater injection was temporarily stopped in order to refill the valve pit with seawater using a variety of emergency service and JSDF vehicles. However, the process to restart seawater injection was interrupted by another explosion in the unit 3 RB at 11:01 which damaged water lines and prompted another evacuation. Injection of seawater into unit 1 would not resume until that evening, after 18 hours without cooling.

Subsequent analysis in November suggested that this extended period without cooling resulted in the melting of the fuel in unit 1, most of which would have escaped the reactor pressure vessel (RPV) and embedded itself into the concrete at the base of the PCV. Although at the time it was difficult to determine how far the fuel had eroded and diffused into the concrete, it was estimated that the fuel remains within the PCV.

In November 2013, Mari Yamaguchi reported for Associated Press that there are computer simulations that suggest that "the melted fuel in Unit 1, whose core damage was the most extensive, has breached the bottom of the primary containment vessel and even partially eaten into its concrete foundation, coming within about 30 cm (1 ft) of leaking into the ground" – a Kyoto University nuclear engineer said with regard to these estimates: "We just can't be sure until we actually see the inside of the reactors."

TEPCO estimated for Unit 1 that "the decay heat must have decreased enough, the molten fuel can be assumed to remain in PCV (primary containment vessel)".

In February 2015, TEPCO started the muon scanning process for Units 1, 2, and 3. With this scanning setup it was possible to determine the approximate amount and location of the remaining nuclear fuel within the RPV, but not the amount and resting place of the corium in the PCV. In March 2015 TEPCO released the result of the muon scan for Unit 1 which showed that no fuel was visible in the RPV, which would suggest that most if not all of the molten fuel had dropped onto the bottom of the PCV – this will change the plan for the removal of the fuel from Unit 1.

Unit 2

Unit 2 was the only other operating reactor which experienced total loss of AC and DC power. Prior to blackout, the RCIC was functioning as designed without the need for operator intervention. The safety relief valve (SRV) would intermittently release steam directly into the PCV suppression torus at its design pressure and the RCIC properly replenished lost coolant. However, following the total blackout of unit 2, the plant operators (similar to unit 1) assumed the worst-case scenario and prepared for a LOC incident. However, when a team was sent to investigate the status of the RCIC of unit 2 the following morning (02:55), they confirmed that the RCIC was operating with the PCV pressure well below design limits. Based on this information, efforts were focused onto unit 1. However, the condensate storage tank from which the RCIC draws water from was nearly depleted by the early morning, and so the RCIC was manually reconfigured at 05:00 to recirculate water from the suppression chamber instead.

On the 13th, unit 2 was configured to vent the PCV automatically (manually opening all valves, leaving only the rupture disk) and preparations were made to inject seawater from the valve pit via the FP system should the need arise. However, as a result of the explosion in unit 3 the following day, the seawater injection setup was damaged and the isolation valve for the PCV vent was found to be closed and inoperable.

At 13:00 on the 14th, the RCIC pump for unit 2 failed after 68 hours of continuous operation. With no way to vent the PCV, in response, a plan was devised to delay containment failure by venting the reactor vessel into the PCV using the SRV in order to allow for seawater injection into the reactor vessel.

The following morning (March 15, 06:15), another explosion was heard on site coinciding with a rapid drop of suppression chamber pressure to atmospheric pressure, interpreted as a malfunction of suppression chamber pressure measurement. Due to concerns about the growing radiological hazard on site, almost all workers evacuated to the Fukushima Daini Nuclear Power Plant.

In February 2017, six years after the accident, radiation levels inside the Unit 2 containment building were crudely estimated to be about 650 Sv/h. The estimation was revised later to 80 Sv/h. These readings were the highest recorded since the accident occurred in 2011 and the first recorded in that area of the reactor since the meltdowns. Images showed a hole in metal grating beneath the reactor pressure vessel, suggesting that melted nuclear fuel had escaped the vessel in that area.

In February 2017, TEPCO released images taken inside unit 2 by a remote-controlled camera that show a 2 m (6.5 ft) wide hole in the metal grating under the pressure vessel in the reactor's primary containment vessel, which could have been caused by fuel escaping the pressure vessel, indicating a meltdown/melt-through had occurred, through this layer of containment. Ionizing radiation levels of about 210 sieverts (Sv) per hour were subsequently detected inside the Unit 2 containment vessel. Undamaged spent fuel typically has values of 270 Sv/h, after ten years of cold shutdown with no shielding.

In January 2018, a remote-controlled camera confirmed that nuclear fuel debris was at the bottom of the Unit 2 PCV, showing fuel had escaped the RPV. The handle from the top of a nuclear fuel assembly was also observed, confirming that a considerable amount of the nuclear fuel had melted.

Unit 3

Unit 3 after the explosion on 15 March 2011.

Although AC power was lost, some DC power was still available in unit 3 and the workers were able to remotely confirm that the RCIC system was continuing to cool the reactor. However, knowing that their DC supply was limited, the workers managed to extend the backup DC supply to about 2 days by disconnecting nonessential equipment, until replacement batteries were brought from a neighboring power station on the morning of the 13th (with 7 hours between loss and restoration of DC power). At 11:36 the next day, after 20.5 hours of operation, the RCIC system failed. In response, the high pressure coolant injection (HPCI) system was activated to alleviate the lack of cooling while workers continued to attempt to restart the RCIC. Additionally, the FP system was utilized to spray the PCV (mainly the SC) with water in order to slow the climbing temperatures and pressures of the PCV.

On the morning of the 13th (02:42), after DC power was restored by new batteries, the HPCI system showed signs of malfunction. The HPCI isolation valve failed to activate automatically upon achieving a certain pressure. In response, the workers decided to switch off HPCI and begin injection of water via the lower pressure firefighting equipment. However, the workers found that the SRV did not operate to relieve pressure from the reactor vessel in order to allow water injection by the DDFP. In response, workers attempted to restart the HPCI and RCIC systems, but both failed to restart. Following this loss of cooling, workers established a water line from the valve pit in order to inject seawater into the reactor alongside unit 2. However, water could not be injected due to RPV pressures exceeding the pump capability. Similarly, preparations were also made to vent the unit 3 PCV, but PCV pressure was not sufficient to burst the rupture disk.

Later that morning (9:08), workers were able to depressurize the reactor by operating the safety relief valve using batteries collected from nearby automobiles. This was shortly followed by the bursting of the venting line rupture disk and the depressurization of the PCV. Unfortunately, venting was quickly stopped by a pneumatic isolation valve which closed on the vent path due to a lack of compressed air, and venting was not resumed until over 6 hours later once an external air compressor could be installed. Despite this, the reactor pressure was immediately low enough to allow for water injection (borated freshwater, as ordered by TEPCO) using the FP system until the freshwater FP tanks were depleted, at which point the injected coolant was switched to seawater from the valve pit.

Cooling was lost once the valve pit was depleted, but was quickly resumed two hours later (unit 1 cooling was postponed until the valve pit was filled). However, despite being cooled, PCV pressure continued to rise and the RPV water level continued to drop until the fuel became uncovered on the morning of the 14th (6:20), as indicated by a water level gauge, which was followed by workers evacuating the area out of concerns about a possible second hydrogen explosion similar to unit 1.

Shortly after work resumed to reestablish coolant lines, an explosion occurred in the unit 3 RB at 11:01 on March 14, which further delayed unit 1 cooling and damaged unit 3's coolant lines. Work to reestablish seawater cooling directly from the ocean began two hours later, and cooling of unit 3 resumed in the afternoon (approximately 16:00) and continued until cooling was lost once more as a result of site evacuation on the 15th.

In August 2014, TEPCO released a new revised estimate that reactor 3 had a complete melt through in the initial phase of the accident. According to this new estimate within the first three days of the accident the entire core content of reactor 3 had melted through the RPV and fallen to the bottom of the PCV. These estimates were based on a simulation, which indicated that reactor 3's melted core penetrated through 1.2 m (3 ft 11 in) of the PCV's concrete base, and came close to 26–68 cm (10–27 in) of the PCV's steel wall.

Unit 4

The unit 4 reactor building after the explosion. The yellow object is the reactor's removed PCV head. The removed black RPV head with its lifting frame attached is to the left. Both had been removed to allow refueling at the time. The green gantry crane carries fuel between the RPV and the spent fuel pool.

Unit 4 was not fueled at the time, but the unit 4 spent fuel pool (SFP) contained a number of fuel rods.

On 15 March, an explosion was observed at the unit 4 RB during site evacuation. A team later returned to the power station to inspect unit 4, but were unable to do so due to the present radiological hazard. The explosion damaged the fourth floor rooftop area of Unit 4, creating two large holes in a wall of the RB. The explosion was later found to be caused by hydrogen passing to unit 4 from unit 3 through shared pipes.

The following day, on the 16th, an aerial inspection was performed by helicopter which confirmed there was sufficient water remaining in the SFP. On the 20th, water was sprayed into the uncovered SFP, later replaced by a concrete pump truck with a boom on the 22nd.

Unit 5

Unit 5 was fueled and was undergoing a RPV pressure test at the time of the accident, but the pressure was maintained by an external air compressor and the reactor was not otherwise operating. Removal of decay heat using the RCIC was not possible, as the reactor was not producing sufficient steam. However, the water within the RPV proved sufficient to cool the fuel, with the SRV venting into the PCV, until AC power was restored on March 13 using the unit 6 interconnection, allowing the use of the low-pressure pumps of the residual heat removal (RHR) system.

Cold shutdown was achieved in the afternoon on the 20th.

Unit 6

Unit 6 was not operating, and its decay heat was low because it had been in an outage since August 2010.

All but one EDG was disabled by the tsunami, allowing unit 6 to retain AC-powered safety functions throughout the incident. However, because the RHR was damaged, workers decided to activate the make-up water condensate system to maintain the reactor water level until the RHR was restored on the 20th.

Cold shutdown was achieved on the 20th, less than an hour after unit 5.

Central fuel storage areas

On 21 March, temperatures in the fuel pond had risen slightly, to 61 °C (142 °F), and water was sprayed over the pool. Power was restored to cooling systems on 24 March and by 28 March, temperatures were reported down to 35 °C (95 °F).

The town of Namie (population 21,000) was evacuated as a result of the accident.

Evacuation

Radiation hotspot in Kashiwa, February 2012
Map of contaminated areas around the plant (22 March – 3 April 2011)

In the initial hours of the accident, in response to station blackout and uncertainty regarding the cooling status of units 1 and 2, a 2 km radius evacuation of 1,900 residents was ordered at 20:50. However, due to difficulty coordinating with the national government, a 3 km evacuation order of ~6,000 residents and a 10 km shelter-in-place order for 45,000 residents was established nearly simultaneously at 21:23. The following morning (05:44), this evacuation radius was expanded to 10 km by local authorities in response to the unit 1 core damage and plans to vent the PCV later that day. The evacuation radius was further revised at 18:25 to 20 km, involving a total of 78,000 residents, in response to the hydrogen explosion at unit 1. However, miscommunication of this final evacuation order resulted in those within 20 km to shelter in place. Additionally, many municipalities independently ordered evacuations ahead of orders from the national government due to loss of communication with authorities; at the time of the 3 km evacuation order, the majority of residents within the zone had already evacuated.

Due to the multiple overlapping evacuation orders, many residents had evacuated to areas which would shortly be designated as evacuation areas. This resulted in many residents having to move multiple times until they reached an area outside of the final 20 km evacuation zone. 20% of residents who were within the initial 2 km radius had to evacuate more than six times.

Additionally, a 30 km shelter in place order was communicated on the 15th, although some municipalities within this zone had already decided to evacuate their residents. This order was followed by a voluntary evacuation recommendation on the 25th, although the majority of residents had evacuated from the 30 km zone by then. The shelter in place order was lifted on April 22, but the evacuation recommendation remained.

Fatalities

Of an estimated 2,220 patients and elderly who resided within hospitals and nursing homes within the 20 km evacuation zone, 51 fatalities are attributed to the evacuation. There was one suspected death due to radiation, as one person died 4 years later of a lung cancer possibly triggered by it. According to one estimation, more than 2,200 deaths are to be attributed to evacuation-related stress, the vast majority of whom were over the age of 65.

Radionuclide release

Radiation measurements from Fukushima Prefecture, March 2011

The predominant mechanism by which fission products can leave the core during core melt is through vaporization, thus only relatively volatile nuclides mix with the vaporized coolant and can be transported by the flow of gas. This gas can then exit the RPV and into the PCV through small leak paths in imperfections in the RPV, but in a situation in which the RCIC is used, this gas flows through the RCIC system and into the suppression pool, where some of the vaporized or suspended fission products are condensed or captured (scrubbed) by the SC, although some remainder (notably, radioactive noble gasses) will remain vaporized or suspended inside of the PCV. From the PCV, similar to the RPV, some small quantity inevitably leaks through small imperfections in the structure, but the predominant designed path for the escape of suspended radionuclides is through venting of the PCV where they are dispersed by the vent stack. However, if the PCV is compromised, the gas will be released directly into the secondary containment, and the potential loss of the SC function would also increase the concentration of unwanted fission products in the gas.

The fraction of releases associated to certain events is debated, as some of the detected fluctuations in the environment do not strongly correlate with events at the power station.

Comparison of radiation levels for different nuclear events

Once released into the atmosphere, those which remain in a gaseous phase will simply be diluted by the atmosphere, but some which precipitate will eventually settle on land or in the ocean. Thus, the majority (90~99%) of the radionuclides which are deposited are isotopes of iodine and caesium, with a small portion of tellurium, which are almost fully vaporized out of the core due to their low vapor pressure. The remaining fraction of deposited radionuclides are of less volatile elements such as barium, antimony, and niobium, of which less than a percent is evaporated from the fuel.

Quantities of the released material are expressed in terms of the three predominant products released: caesium-137, iodine-131, and xenon-133. Estimates for atmospheric releases range from 7–20 PBq for Cs-137, 100–400 PBq for I-131, and 6,000–12,000 PBq for Xe-133.

Approximately 40–80% of the atmospheric releases were deposited over the ocean.

In addition to atmospheric deposition, there was also a significant quantity of direct releases into groundwater (and eventually the ocean) through leaks of coolant which had been in direct contact with the fuel. Estimates for this release vary from 1 to 5.5 PBq. Although the majority had entered the ocean shortly following the accident, a significant fraction remains in the groundwater and continues to mix with coastal waters.

According to the French Institute for Radiological Protection and Nuclear Safety, the release from the accident represents the most important individual oceanic emissions of artificial radioactivity ever observed. The Fukushima coast has one of the world's strongest currents (Kuroshio Current). It transported the contaminated waters far into the Pacific Ocean, dispersing the radioactivity. As of late 2011 measurements of both the seawater and the coastal sediments suggested that the consequences for marine life would be minor. Significant pollution along the coast near the plant might persist, because of the continuing arrival of radioactive material transported to the sea by surface water crossing contaminated soil. The possible presence of other radioactive substances, such as strontium-90 or plutonium, has not been sufficiently studied. Recent measurements show persistent contamination of some marine species (mostly fish) caught along the Fukushima coast.

Consequences

Evacuation

In January 2015, the number of residents displaced due to the accident was around 119,000, peaking at 164,000 in June 2012. In terms of months of life lost, the loss of life would have been far smaller if all residents had done nothing at all, or were sheltered in place, instead of evacuated.

In the former Soviet Union, many patients with negligible radioactive exposure after the Chernobyl accident displayed extreme anxiety about radiation exposure. They developed many psychosomatic problems, including radiophobia along with an increase in fatalistic alcoholism. As Japanese health and radiation specialist Shunichi Yamashita noted:

We know from Chernobyl that the psychological consequences are enormous. Life expectancy of the evacuees dropped from 65 to 58 years – not because of cancer, but because of depression, alcoholism, and suicide. Relocation is not easy, the stress is very big. We must not only track those problems, but also treat them. Otherwise people will feel they are just guinea pigs in our research.

A 2012 survey by the Iitate local government obtained responses from approximately 1,743 evacuees within the evacuation zone. The survey showed that many residents are experiencing growing frustration, instability, and an inability to return to their earlier lives. Sixty percent of respondents stated that their health and the health of their families had deteriorated after evacuating, while 39.9% reported feeling more irritated compared to before the accident.

Summarizing all responses to questions related to evacuees' current family status, one-third of all surveyed families live apart from their children, while 50.1% live away from other family members (including elderly parents) with whom they lived before the disaster. The survey also showed that 34.7% of the evacuees have suffered salary cuts of 50% or more since the outbreak of the nuclear disaster. A total of 36.8% reported a lack of sleep, while 17.9% reported smoking or drinking more than before they evacuated.

Stress often manifests in physical ailments, including behavioral changes such as poor dietary choices, lack of exercise, and sleep deprivation. Survivors, including some who lost homes, villages, and family members, were found likely to face mental health and physical challenges. Much of the stress came from lack of information and from relocation.

A 2014 metareview of 48 articles indexed by PubMed, PsycINFO, and EMBASE, highlighted several psychophysical consequences among the residents in Miyagi, Iwate, Ibaraki, Tochigi and Tokyo. The resulting outcomes included depressive symptoms, anxiety, sleep disturbance, social functioning, social isolation, admission rates, suicide rates and cerebral structure changes, radiation impacting food safety, maternal anxiety and lowered maternal confidence. The rates of psychological distress among evacuated people rose fivefold compared to the Japanese average due to the experience of the accident and evacuation. An increase in childhood obesity in the area after the accident has also been attributed to recommendations that children stay indoors instead of going outside to play.

Worldwide media coverage of the incident has been described as "ten years of disinformation", with media and environmental organizations routinely conflating the casualties of the earthquake and tsunami, with casualties of the nuclear incident. The incident dominated media coverage while the victims of the natural disasters were "ignored", and a number of media reports incorrectly describing thousands of victims of tsunami as if they were victims of the "nuclear disaster".

Anti-nuclear power plant rally on 19 September 2011 at the Meiji Shrine complex in Tokyo
Electricity generation by source in Japan (month-level data). Nuclear energy's contribution declined steadily throughout 2011 due to shutdowns and has been mainly replaced with thermal power stations such as fossil gas and coal power plants.
The use of nuclear power (in yellow) in Japan declined significantly after the Fukushima accident.
The number of nuclear power plant constructions started each year worldwide, from 1954 to 2013. Following an increase in new constructions from 2007 to 2010, there was a decline after the Fukushima nuclear accident.

Energy policy

Part of the Seto Hill Windfarm in Japan, one of several windfarms that continued generating without interruption after the 2011 earthquake and tsunami and the Fukushima nuclear accident
Price of solar panels (yen/Wp) in Japan

Prior to the accident, over 25% of domestic electricity generation in Japan utilized nuclear power and Japan had set a fairly ambitious GHG reduction target of 25% below 1990 levels by 2020, which involved increasing the share of nuclear power in electricity generation from 30% to 50%. However, this plan was abandoned and target was quickly revised to a 3% emissions increase by 2020 following the accident, alongside a focus on reducing dependence on nuclear power in favor of improved thermal efficiency in fossil fuel energy use and increasing the share of "renewables". The contribution of nuclear energy dropped to less than a percent following the accident and all nuclear reactors in the country were shut down by 2013. This resulted in an increase in the share of fossil fuel energy use, which had increased to ~94% by 2015 (the highest of any IEA member state, with the remaining ~6% produced by renewables, an increase from 4% in 2010). The required fossil fuel imports in 2011 resulted in a trade deficit for the first time in decades which would continue in the following decade.

In the immediate aftermath, nine prefectures served by TEPCO experienced power rationing. The government asked major companies to reduce power consumption by 15%, and some shifted their weekends to weekdays to smooth power demand. As of 2013, TEPCO and eight other Japanese power companies were paying approximately 3.6 trillion JPY (37 billion USD) more in combined imported fossil fuel costs compared to 2010 to make up for the missing power.

Elections

On 16 December 2012, Japan held its general election. The Liberal Democratic Party (LDP) had a clear victory, with Shinzō Abe as the new Prime Minister. Abe supported nuclear power, saying that leaving the plants closed was costing the country 4 trillion yen per year in higher costs. The comment came after Junichiro Koizumi, who chose Abe to succeed him as premier, made a statement to urge the government to take a stance against using nuclear power. A survey on local mayors by the Yomiuri Shimbun newspaper in 2013 found that most of them from cities hosting nuclear plants would agree to restarting the reactors, provided the government could guarantee their safety. More than 30,000 people marched on 2 June 2013, in Tokyo against restarting nuclear power plants. Marchers had gathered more than 8 million petition signatures opposing nuclear power.

Previously a proponent of building more reactors, Prime Minister Naoto Kan took an increasingly anti-nuclear stance following the accident. In May 2011, he ordered the aging Hamaoka Nuclear Power Plant closed over earthquake and tsunami concerns, and said he would freeze building plans. In July 2011, Kan said, "Japan should reduce and eventually eliminate its dependence on nuclear energy".

International Impact

In the aftermath, Germany accelerated plans to close its nuclear power reactors and decided to phase the rest out by 2022 (see also Nuclear power in Germany). Belgium and Switzerland have also changed their nuclear policies to phase-out all nuclear energy operations. Italy held a national referendum, in which 94 percent voted against the government's plan to build new nuclear power plants. In France, President Hollande announced the intention of the government to reduce nuclear usage by one third. However, the government earmarked only one power station for closure – the aging Fessenheim Nuclear Power Plant on the German border – which prompted some to question the government's commitment to Hollande's promise. Industry Minister Arnaud Montebourg is on record as saying that Fessenheim will be the only nuclear power station to close. On a visit to China in December 2014 he reassured his audience that nuclear energy was a "sector of the future" and would continue to contribute "at least 50%" of France's electricity output. Another member of Hollande's Socialist Party, the MP Christian Bataille, said that Hollande announced the nuclear curb to secure the backing of his Green coalition partners in parliament.

China suspended its nuclear development program briefly, but restarted it shortly afterwards. The initial plan had been to increase the nuclear contribution from 2 to 4 percent of electricity by 2020, with an escalating program after that. Renewable energy supplies 17 percent of China's electricity, 16% of which is hydroelectricity. China plans to triple its nuclear energy output to 2020, and triple it again between 2020 and 2030.

New nuclear projects were proceeding in some countries. KPMG reports 653 new nuclear facilities planned or proposed for completion by 2030. By 2050, China hopes to have 400–500 gigawatts of nuclear capacity – 100 times more than it has now. The Conservative Government of the United Kingdom is planning a major nuclear expansion despite some public objection. So is Russia. India is also pressing ahead with a large nuclear program, as is South Korea. Indian Vice President M Hamid Ansari said in 2012 that "nuclear energy is the only option" for expanding India's energy supplies, and Prime Minister Modi announced in 2014 that India intended to build 10 more nuclear reactors in a collaboration with Russia.

In the wake of the accident, the Senate Appropriations Committee requested the United States Department of Energy “to give priority to developing enhanced fuels and cladding for light water reactors to improve safety in the event of accidents in the reactor or spent fuel pools”. This brief has led to ongoing research and development of Accident Tolerant Fuels, which are specifically designed to withstand the loss of cooling for an extended period, increase time to failure, and increase fuel efficiency. This is accomplished by incorporating specially designed additives to standard fuel pellets and replacing or altering the fuel cladding in order to reduce corrosion, decrease wear, and reduce hydrogen generation during accident conditions. While research is still ongoing, on 4 March 2018, the Edwin I. Hatch Nuclear Power Plant near Baxley, Georgia has implemented “IronClad” and “ARMOR” (Fe-Cr-Al and coated Zr claddings, respectively) for testing.

Radiation effects in humans

Seawater-contamination along coast with Caesium-137, from 21 March until 5 May 2011 (Source: GRS)

Radiation exposure of those living in proximity to the accident site is expected to be below 10 mSv, over the course of a lifetime. In comparison, the dosage of background radiation received over a lifetime is 170 mSv. Very few cancers are expected as a result of accumulated radiation exposures and residents who were evacuated were exposed to so little radiation that radiation-induced health effects were likely to be below detectable levels. There is no increase in miscarriages, stillbirths or physical and mental disorders in babies born after the accident.

Outside the geographical areas most affected by radiation, even in locations within Fukushima prefecture, the predicted risks remain low, and no observable increases in cancer above natural variation in baseline rates are anticipated.

— World Health Organization, 2013

Estimated effective doses outside Japan are considered to be below (or far below) the levels regarded as very small by the international radiological protection community. The Integrated Fukushima Ocean Radionuclide Monitoring project (InFORM) failed to show any significant amount of radiation and as a result its authors received death threats from supporters of a "wave of cancer deaths across North America" theory.

Thyroid cancer

The overwhelming majority of thyroid growths are benign growths that will never cause symptoms, illness, or death, even if nothing is ever done about the growth. Autopsy studies on people who died from other causes show that more than one third of adults technically have a thyroid growth/cancer. As a precedent, in 1999 in South Korea, the introduction of advanced ultrasound thyroid examinations resulted in an explosion in the rate of benign thyroid cancers being detected and needless surgeries occurring. Despite this, the death rate from thyroid cancer has remained the same.

There is a statistically significant correlation between external radiation dose and thyroid cancer in those under the age of 18. However, this is mostly attributable to the early detection of non-symptomatic disease cases by the screening-effect. Rates of thyroid cancer in children controlled for examination frequency showed no association between the nuclear accident/radiation exposure and thyroid cancer.

As of 2020, research into the correlation between air-dose and internal-dose and thyroid cancers remains ongoing. Further research is necessary in understanding the dose-response relationship and the prevalence of incident cancers.

Thyroid cancer is one of the most survivable cancers, with an approximate 94% survival rate after first diagnosis. That rate increases to a nearly 100% survival rate if caught early. Cancer may spread to another part of the body, however, and in cases where the thyroid must be removed, the resulting hormonal deficiencies are terminal. In January 2022, six such patients who were children at the time of the accident sued TEPCO for 616 million yen after developing thyroid cancer.

Infant/fetal cancer risk

Evacuated infant girls, the most radiation-sensitive demographic, have an estimated increased lifetime risk of developing thyroid cancer of 1.25% (compared to 0.75% background risk), with the increase being slightly less for males. The risks from a number of additional radiation-induced cancers are also expected to be elevated. There is an estimated 7% higher relative risk of leukemia in males exposed as infants and a 6% higher relative risk of breast cancer in females exposed as infants. In total, an overall 1% higher lifetime risk of developing cancers of all types is predicted for infant females, with the risk slightly lower for males. The fetuses, depending on their sex, would have the same elevations in risk as the infant groups.

Linear no-threshold models (LNT)

LNT models estimate that the accident would most likely cause 130 cancer deaths. However, LNT models have large uncertainties and are not useful for estimating health effects from radiation especially when the effects of radiation on the human body are not linear, and with obvious thresholds. Producing a statistically useful estimate would require an impractically large number of patients, and LNT models have been described as "junk science". In September 2018, one cancer fatality was the subject of a financial settlement, to the family of a former nuclear station workman.

Radiation effects in non-humans

On 21 March, the first restrictions were placed on the distribution and consumption of contaminated items. However, the results of measurements of both the seawater and the coastal sediments led to the supposition that the consequences of the accident, in terms of radioactivity, would be minor for marine life as of autumn 2011. Despite caesium isotopic concentrations in the waters off of Japan being 10 to 1000 times above the normal concentrations prior to the accident, radiation risks are below what is generally considered harmful to marine animals and human consumers.

As of March 2012, no cases of radiation-related ailments had been reported.

Calculated caesium-137 concentration in the air, 19 March 2011

Fisheries

Organisms that filter water and fish at the top of the food chain are, over time, the most sensitive to caesium pollution. It is thus justified to maintain surveillance of marine life that is fished in the coastal waters off Fukushima. Migratory pelagic species are also highly effective and rapid transporters of pollutants throughout the ocean. Elevated levels of Cs-134 appeared in migratory species off the coast of California that were not seen prior to the accident.

In April 2014, studies confirmed the presence of radioactive tuna off the coasts of the Pacific U.S. Researchers carried out tests on 26 albacore tuna caught prior to the 2011 power plant accident and those caught after. However, the amount of radioactivity is less than that found naturally in a single banana. Cs-137 and Cs-134 have been noted in Japanese whiting in Tokyo Bay as of 2016. "Concentration of radiocesium in the Japanese whiting was one or two orders of magnitude higher than that in the sea water, and an order of magnitude lower than that in the sediment." They were still within food safety limits.

In June 2016, the political advocacy group "International Physicians for the Prevention of Nuclear War", asserted that 174,000 people have been unable to return to their homes and ecological diversity has decreased and malformations have been found in trees, birds, and mammals. Although physiological abnormalities have been reported within the vicinity of the accident zone, the scientific community has largely rejected any such findings of genetic or mutagenic damage caused by radiation, instead showing it can be attributed either to experimental error or other toxic effects.

In February 2018, Japan renewed the export of fish caught off Fukushima's nearshore zone. According to prefecture officials, no seafood had been found with radiation levels exceeding Japan safety standards since April 2015. In 2018, Thailand was the first country to receive a shipment of fresh fish from Japan's Fukushima prefecture. A group campaigning to help prevent global warming has demanded the Food and Drug Administration disclose the name of the importer of fish from Fukushima and of the Japanese restaurants in Bangkok serving it. Srisuwan Janya, chairman of the Stop Global Warming Association, said the FDA must protect the rights of consumers by ordering restaurants serving Fukushima fish to make that information available to their customers, so they could decide whether to eat it or not.

In February 2022, Japan suspended the sale of black rockfish from Fukushima after it was discovered that one fish from Soma had 180 times more radioactive Cesium-137 than legally permitted. The high levels of radioactivity led investigators to believe it had escaped from a breakwater at the accident site, despite nets intended to prevent fish from leaving the area. A total of 44 other fish from the accident site show similar levels.

Remediation and recovery

IAEA team examining Unit 3

To assuage fears, the government enacted an order to decontaminate over a hundred areas where the level of additional radiation was greater than one millisievert per year. This is a much lower threshold than is necessary for protecting health. The government also sought to address the lack of education on the effects of radiation and the extent to which the average person was exposed.

In 2018, tours to visit the accident area began. In September 2020, The Great East Japan Earthquake and Nuclear Disaster Memorial Museum was opened in the town of Futaba, near the power plant. The museum exhibits items and videos about the earthquake and the nuclear accident. To attract visitors from abroad, the museum offers explanations in English, Chinese and Korean.

Tokyo Electric Power Company (TEPCO) is going to remove the remaining nuclear fuel material from the plants. TEPCO completed the removal of 1535 fuel assemblies from the Unit 4 spent fuel pool in December 2014 and 566 fuel assemblies from the Unit 3 spent fuel pool in February 2021. TEPCO plans to remove all fuel rods from the spent fuel pools of Units 1, 2, 5, and 6 by 2031 and to remove the remaining molten fuel debris from the reactor containments of Units 1, 2, and 3 by 2040 or 2050. An ongoing intensive cleanup program to both decontaminate affected areas and decommission the plant will take 30 to 40 years from the accident, plant management estimated.

Treating contaminated water

As of 2013, about 400 metric tons (390 long tons; 440 short tons) of cooling water per day was being pumped into the reactors. Another 400 metric tons (390 long tons; 440 short tons) of groundwater was seeping into the structure. Some 800 metric tons (790 long tons; 880 short tons) of water per day was removed for treatment, half of which was reused for cooling and half diverted to storage tanks. Ultimately the contaminated water, after treatment to remove radionuclides other than tritium, has to be discharged into the Pacific. TEPCO decided to create an underground ice wall to block the flow of groundwater into the reactor buildings. A $300 million 7.8 MW cooling facility freezes the ground to a depth of 30 meters. As of 2019, the contaminated water generation had been reduced to 170 metric tons (170 long tons; 190 short tons) per day.

In February 2014, NHK reported that TEPCO was reviewing its radioactivity data, after finding much higher levels of radioactivity than was reported earlier. TEPCO now says that levels of 5 MBq (0.12 millicuries) of strontium per liter (23 MBq/imp gal; 19 MBq/U.S. gal; 610 μCi/imp gal; 510 μCi/U.S. gal) were detected in groundwater collected in July 2013 and not the 900 kBq (0.02 millicuries) (4.1 MBq/imp gal; 3.4 MBq/U.S. gal; 110 μCi/imp gal; 92 μCi/U.S. gal) that were initially reported.

On 10 September 2015, floodwaters driven by Typhoon Etau prompted mass evacuations in Japan and overwhelmed the drainage pumps at the stricken power plant. A TEPCO spokesperson said that hundreds of metric tons of radioactive water entered the ocean as a result. Plastic bags filled with contaminated soil and grass were also swept away by the flood waters.

As of October 2019, 1.17 million cubic meters of contaminated water was stored in the plant area. The water is being treated by a purification system that can remove radionuclides, except tritium, to a level that Japanese regulations allow to be discharged to the sea. As of December 2019, 28% of the water had been purified to the required level, while the remaining 72% needed additional purification. However, tritium cannot be separated from the water. As of October 2019, the total amount of tritium in the water was about 856 terabecquerels, and the average tritium concentration was about 0.73 megabecquerels per liter.

A committee set up by the Japanese Government concluded that the purified water should be released to the sea or evaporated to the atmosphere. The committee calculated that discharging all the water to the sea in one year would cause a radiation dose of 0.81 microsieverts to the local people, whereas evaporation would cause 1.2 microsieverts. For comparison, Japanese people get 2100 microsieverts per year from natural radiation. IAEA considers that the dose calculation method is appropriate. Further, the IAEA recommends that a decision on the water disposal must be made urgently.

Despite the negligible doses, the Japanese committee is concerned that the water disposal may cause reputational damage to the prefecture, especially to the fishing industry and tourism.

Tanks used to store the water are expected to be filled in 2023. In July 2022, Japan's Nuclear Regulation Authority approved discharging the treated water into the sea. A US State Department spokesperson supported the decision. South Korea's foreign minister and activists from Japan and South Korea protested the announcement. In April 2023, fishers and activists held protests in front of the Japanese embassy in the Philippines in opposition to the planned release of 1.3 million tons of treated water into the Pacific Ocean. On 22 August, Japan announced that it would start releasing treated radioactive water from the tsunami-hit Fukushima nuclear plant into the Pacific Ocean in 48 hours, despite opposition from its neighbours. Japan says the water is safe, many scientists agree, and the decision comes weeks after the UN's nuclear watchdog approved the plan; but critics say more studies need to be done and the release should be halted. On 24 August, Japan begun the discharge of treated waste water into the Pacific Ocean, sparking protests in the region and retaliation from China, who said it would block all imports of seafood from Japan.

Other radioactive substances created as a byproduct of the contaminated water purification process, as well as contaminated metal from the damaged plant, have drawn recent attention as the 3,373 waste storage containers for the radioactive slurry were found to be degrading faster than expected.

Compensation and government expenses

Initial estimates of costs to Japanese taxpayers were in excess of 12 trillion yen ($100 billion). In December 2016 the government estimated decontamination, compensation, decommissioning, and radioactive waste storage costs at 21.5 trillion yen ($187 billion), nearly double the 2013 estimate. By 2021 12.1 trillion yen had already been spent, with 7 trillion yen on compensation, 3 trillion yen on decontamination, and 2 trillion yen on decommissioning and storage. Despite concerns, the government expected total costs to remain under budget.

The amount of compensation to be paid by TEPCO is expected to reach 7 trillion yen.

In March 2017, a Japanese court ruled that negligence by the Japanese government had led to the Fukushima accident by failing to use its regulatory powers to force TEPCO to take preventive measures. The Maebashi district court near Tokyo awarded ¥39 million (US$345,000) to 137 people who were forced to flee their homes following the accident. On 30 September 2020, the Sendai High Court ruled that the Japanese government and TEPCO are responsible for the accident, ordering them to pay $9.5 million in damages to residents for their lost livelihoods. In March 2022, Japan's Supreme Court rejected an appeal from TEPCO and upheld the order for it to pay damages 1.4 billion yen ($12 million) to about 3,700 people whose lives were harmed by the accident. Its decision covered three class-action lawsuits, among more than 30 filed against the utility.

On 17 June 2022, the Supreme Court acquitted the government of any wrongdoing regarding potential compensation to over 3,700 people affected by the accident.

On 13 July 2022, four former TEPCO executives were ordered to pay 13 trillion yen ($95 billion) in damages to the operator of power plant, in the civil case brought by Tepco shareholders.

Equipment, facility, and operational changes

A number of nuclear reactor safety system lessons emerged from the incident. The most obvious was that in tsunami-prone areas, a power station's sea wall must be adequately tall and robust. At the Onagawa Nuclear Power Plant, closer to the epicenter of 11 March earthquake and tsunami, the sea wall was 14 meters (46 ft) tall and successfully withstood the tsunami, preventing serious damage and radioactivity releases.

Nuclear power station operators around the world began to install passive autocatalytic recombiners ("PARs"), which do not require electricity to operate. PARs work much like the catalytic converter on the exhaust of a car to turn potentially explosive gases such as hydrogen into water. Had such devices been positioned at the top of the reactor buildings, where hydrogen gas collected, the explosions would not have occurred and the releases of radioactive isotopes would arguably have been much less.

Unpowered filtering systems on containment building vent lines, known as Filtered Containment Venting Systems (FCVS), can safely catch radioactive materials and thereby allow reactor core depressurization, with steam and hydrogen venting with minimal radioactivity emissions. Filtration using an external water tank system is the most common established system in European countries, with the water tank positioned outside the containment building. In October 2013, the owners of Kashiwazaki-Kariwa nuclear power station began installing wet filters and other safety systems, with completion anticipated in 2014.

For generation II reactors located in flood or tsunami prone areas, a 3+ day supply of back-up batteries has become an informal industry standard. Another change is to harden the location of back-up diesel generator rooms with water-tight, blast-resistant doors and heat sinks, similar to those used by nuclear submarines. The oldest operating nuclear power station in the world, Beznau, which has been operating since 1969, has a 'Notstand' hardened building designed to support all of its systems independently for 72 hours in the event of an earthquake or severe flooding. This system was built prior to Fukushima Daiichi.

Upon a station blackout, similar to the one that occurred after back-up battery supply was exhausted, many constructed Generation III reactors adopt the principle of passive nuclear safety. They take advantage of convection (hot water tends to rise) and gravity (water tends to fall) to ensure an adequate supply of cooling water to handle the decay heat, without the use of pumps.

As the crisis unfolded, the Japanese government sent a request for robots developed by the U.S. military. The robots went into the plants and took pictures to help assess the situation, but they couldn't perform the full range of tasks usually carried out by human workers. The accident illustrated that robots lacked sufficient dexterity and robustness to perform critical tasks. In response to this shortcoming, a series of competitions were hosted by DARPA to accelerate the development of humanoid robots that could supplement relief efforts. Eventually a wide variety of specially designed robots were employed (leading to a robotics boom in the region), but as of early 2016 three of them had promptly become non-functional due to the intensity of the radioactivity; one was destroyed within a day.

Criticism

Prior safety concerns

On 5 July 2012, the NAIIC found that the causes of the accident had been foreseeable, and that the plant operator (TEPCO) had failed to meet basic safety requirements such as risk assessment, preparing for containing collateral damage, and developing evacuation plans. At a meeting in Vienna three months after the accident, the IAEA faulted lax oversight by the Japanese Ministry of Economy, Trade and Industry, saying the ministry faced an inherent conflict of interest as the government agency in charge of both regulating and promoting the nuclear power industry. On 12 October 2012, TEPCO admitted that it had failed to take necessary measures for fear of inviting lawsuits or protests against its nuclear plants.

Unit 1 EDG disabled by flooding in 1991

On 30 October 1991, one of unit 1's EDGs failed as a result of a condensate coolant leak in the turbine building, as reported by former employees in December 2011. A TEPCO report in 2011 detailed that the room was flooded through a door and some holes for cables, but the power supply was not cut off by the flooding. An engineer was quoted as saying that he informed his superiors of the possibility that a tsunami could damage the generators.

In response, TEPCO installed doors to prevent water from leaking into the generator rooms. The JNSC stated that it would revise its safety guidelines and would require the installation of additional power sources.

Tsunami studies

In 1991, the U.S. Nuclear Regulatory Commission warned of a risk of losing emergency power in 1991 (NUREG-1150) and NISA referred to that report in 2004, but took no action to mitigate the risk.

In 2000, an in-house TEPCO report recommended safety measures against seawater flooding, based on the potential of a 50 foot (15 m) tsunami. TEPCO did not act due to concerns about creating anxieties over the safety of the nuclear power plant.

In 2002, the government earthquake research headquarters estimated that a tsunami up to 15.7 meters (52 ft) could hit the power station.

In 2004, the cabinet office warned that tsunamis taller than the maximum of 5.6 meters (18 ft) forecast by TEPCO and government officials were possible.

In 2008, another in-house study identified an immediate need to better protect the facility from flooding by seawater which cited the 15.7 meters (52 ft) estimate from the 2002 study.

In 2009, the Active Fault and Earthquake Research Center urged TEPCO and NISA to revise their assumptions for possible tsunami heights upwards, based on his team's findings about the 869 Sanriku earthquake, but this was not seriously considered at the time.

Communications

Many criticisms have been made which claim that the evacuation zone should have been further expanded, namely regarding the limited proliferation of data which governments of less affected areas may have acted upon. The national government only sent data from the SPEEDI network to the Fukushima prefectural government and was later criticized for delaying the communication of data to the U.S. military. Additionally, the U.S. military produced a detailed map using aircraft and provided it to the Ministry of Economy, Trade and Industry (METI) on 18 March and to the Ministry of Education, Culture, Sports, Science and Technology (MEXT) two days later, but no new evacuation plans were made a week after the accident. The data was not sent to the prime minister or the Nuclear Safety Commission, for which the government was criticized, but was made accessible to the public on the 23rd.

Record-keeping

The Japanese government did not keep records of key meetings during the crisis. Emails from NISA to the Fukushima prefectural government, including evacuation and health advisories from 12 March 11:54 PM to 16 March 9 AM, went unread and were deleted.

On 14 March 2011 TEPCO officials were instructed not to use the phrase "core meltdown" at press conferences.

Japan towns, villages, and cities in and around the Daiichi nuclear plant exclusion zone. The 20 and 30 km (12 and 19 mi) areas had evacuation and shelter in place orders, and additional administrative districts that had an evacuation order are highlighted. However, the above map's factual accuracy is called into question as only the southern portion of Kawamata district had evacuation orders. More accurate maps are available.

International reaction

IAEA experts at Unit 4, 2013
Evacuation flight departs Misawa.
U.S. Navy humanitarian flight undergoes radioactive decontamination.
Protest against nuclear power in Cologne, Germany on 26 March 2011

The international reaction to the accident was diverse and widespread. Many inter-governmental agencies immediately offered help, often on an ad hoc basis. Responders included IAEA, World Meteorological Organization and the Preparatory Commission for the Comprehensive Nuclear Test Ban Treaty Organization.

In May 2011, UK chief inspector of nuclear installations Mike Weightman traveled to Japan as the lead of an International Atomic Energy Agency (IAEA) expert mission. The main finding of this mission, as reported to the IAEA ministerial conference that month, was that risks associated with tsunamis in several sites in Japan had been underestimated.

In September 2011, IAEA Director General Yukiya Amano said the Japanese nuclear disaster "caused deep public anxiety throughout the world and damaged confidence in nuclear power". Following the accident, it was reported in The Economist that the IAEA halved its estimate of additional nuclear generating capacity to be built by 2035.

Investigations

TEPCO released estimates of the state and location of the fuel in a November 2011 report. The report concluded that the Unit 1 RPV was damaged during the accident and that "significant amounts" of molten fuel had fallen into the bottom of the PCV. The erosion of the concrete of the PCV by the molten fuel after the core meltdown was estimated to stop at approx. 0.7 m (2 ft 4 in) in depth, while the thickness of the containment floor is 7.6 m (25 ft). Gas sampling carried out before the report detected no signs of an ongoing reaction of the fuel with the concrete of the PCV and all the fuel in Unit 1 was estimated to be "well cooled down, including the fuel dropped on the bottom of the reactor". Fuel in Units 2 and 3 had melted, however less than in Unit 1. The report further suggested that "there is a range in the evaluation results" from "all fuel in the RPV (none fuel fallen to the PCV)" in Unit 2 and Unit 3, to "most fuel in the RPV (some fuel in PCV)". For Unit 2 and Unit 3 it was estimated that the "fuel is cooled sufficiently". According to the report, the greater damage in Unit 1 (when compared to the other two units) was due to the longer time that no cooling water was injected in Unit 1. This resulted in much more decay heat accumulating, as for about 1 day there was no water injection for Unit 1, while Unit 2 and Unit 3 had only a quarter of a day without water injection.

Three investigations into the accident showed the man-made nature of the catastrophe and its roots in regulatory capture associated with a "network of corruption, collusion, and nepotism." A New York Times report found that the Japanese nuclear regulatory system consistently sided with, and promoted, the nuclear industry based on the concept of amakudari ('descent from heaven'), in which senior regulators accepted high paying jobs at companies they once oversaw.

In August 2011, several top energy officials were fired by the Japanese government; affected positions included the Vice-minister for Economy, Trade and Industry; the head of the Nuclear and Industrial Safety Agency, and the head of the Agency for Natural Resources and Energy.

In 2016 three former TEPCO executives, chairman Tsunehisa Katsumata and two vice presidents, were indicted for negligence resulting in death and injury. In June 2017 the first hearing took place, in which the three pleaded not guilty to professional negligence resulting in death and injury. In September 2019 the court found all three men not guilty.

NAIIC

The Fukushima Nuclear Accident Independent Investigation Commission (NAIIC) was the first independent investigation commission by the National Diet in the 66-year history of Japan's constitutional government.

The accident "cannot be regarded as a natural disaster," the NAIIC panel's chairman, Tokyo University professor emeritus Kiyoshi Kurokawa, wrote in the inquiry report. "It was a profoundly man-made accident – that could and should have been foreseen and prevented. And its effects could have been mitigated by a more effective human response." "Governments, regulatory authorities and Tokyo Electric Power [TEPCO] lacked a sense of responsibility to protect people's lives and society," the Commission said. "They effectively betrayed the nation's right to be safe from nuclear accidents. He stated that the accident was "made in Japan", since it was a manifestation of certain cultural traits, saying:

“Its fundamental causes are to be found in the ingrained conventions of Japanese culture: our reflexive obedience; our reluctance to question authority; our devotion to ‘sticking with the program’; our groupism; and our insularity.”

The Commission recognized that the affected residents were still struggling and facing grave concerns, including the "health effects of radiation exposure, displacement, the dissolution of families, disruption of their lives and lifestyles and the contamination of vast areas of the environment".

Investigation committee

The purpose of the Investigation Committee on the Accident at the Fukushima Nuclear Power Stations (ICANPS) was to identify the accident's causes and propose policies designed to minimize the damage and prevent the recurrence of similar incidents. The 10 member, government-appointed panel included scholars, journalists, lawyers, and engineers. It was supported by public prosecutors and government experts and released its final 448-page investigation report on 23 July 2012.

The panel's report faulted an inadequate legal system for nuclear crisis management, a crisis-command disarray caused by the government and TEPCO, and possible excess meddling on the part of the Prime Minister's office in the crisis' early stage. The panel concluded that a culture of complacency about nuclear safety and poor crisis management led to the nuclear accident.

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